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@@ -447,7 +447,7 @@ And when doing heated inserts make sure to do a couple of extra wall layers. So
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## Testing the drone(V1)
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The first test of the drone went horribly wrong. This was a first test with analog control with not stabilization feedback from the IMU to see if it would come off the ground.
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The first test of the drone went horribly wrong. This was a first test with analog control with not stabilization feedback from the IMU to see if it would come off the ground. Sadly it did not go as expected.
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<video controls src="../PXL_20250604_121528011(1).mp4" title="Title"></video>
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### What went wrong
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@@ -478,7 +478,7 @@ One matrix board got a few ripped of leds and capacitors but I think I am able t
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Luckily we placed cardboard under the drone incase something would happen. The propellors completely mauled the cardboard away where it hit.
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Now that the drone is ripped into several pieces I will be abandoning this design and start from scratch on a second design.
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Now that the drone is ripped into several pieces I will be abandoning this design and start from scratch on a second design. From this point on I can only go up.
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## BOM (bill of materials)
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